Like Dr. Frankenstein while waking up his monster the first time we felt as the printer was connected the frist time to the power supply and the motors started to turn on command....
Working on the last saturday started with soldering the connectors, because all connections between motors and sensors must be done.
We used CV Connectors with 1/10th inch grid, just like the ones used at RC models. Matching connectors are on the RAMPS. So everything should fit.
The connectors are little pieces of platic, the contacs came on a long ribbon. So we need the soldering iron first.
The motors are connected with 4 contact, all the sensors used 2. Everything fine and clear.
| Ramps with (nealry) all cables |
| everything connected - except the display |
| X carriage and extruder |
By coincidence i came to a (real) hardware store (Eisenwarenladen in german) where i got the screws! I was really happy about that.
With this we can also connect the fan which should cool the print and the printhead to save the X carriage / extruder.
| Install the firmware |
Before the firmware can be send to the printer, there are a lot of adjustments to do because every printer is different. The main part can be configured on the homepage of the repetier firmware, after this is done the whole firmware or only the configuration can be downloaded.
Some points can't be configured there, e.g. the heated bed. Therefore you must edit the configuration.h file by hand. If anybody is interested in our config file i will be happy to send it by mail.
We have configured the software to use the EEPROM, with this many of the configuration settings are saved into a non volatile memory into the Arduino. if the EEPROM is not used it is necessary to edit the configuration.h, compile the firmware and install it every time you edit a setting. So the EEPROM make life easier.
| i'm meltinnnnggg...... slightly out of focus |
Directly after this check we set the whole thing on power.Now we can control the motors by software and let them run thru the printspace. Movement in Z axis was very slow, it was set to 2 mm per second to waiting while its moving the whole 300 mm was a pita. Later we speeded it up to 4mm / second.
The tests showed that a few motors are running into the wrong direction. The Z motors and the extruder motor. So we had to possibilities. First we could turn the connectors on the Ramps or second to set an entry into the firmware. We wanted all connectors to be in the same direction so we use the software way.
After some time playing with it, we tried to calibrate the printer. The dimensions were already saved into the firmware in a rough way. But there are some variables which must be tried on the printer.
Nophead has an excellent description how to do this onto his webside.
| Fertig zum Druck |
Heated bed got heated, first try with 55°C, then the hotend (230°C). Filament is moving, the hotend rushes over the printbed, drawing lines onto the printbed. But there is not really plastics on the bed.... so for the next try we move the head about 2/10mm higher. Next try, fine blue lines on the printbed, looks good but we don't have adhesion and the whole extruded material is pulled away with the hotend.
So we made some tape on the printbed. This time the plastics stick on the bed, but we had a massive warping. Rising the temperature of the heated bed to 110°C helps, but it still warps.
So the first tries weren't successful. Its getting late and we decided to stop for this day.
No success but a lot of hope. The prints we could see are looking really nice. We only need some fine tuning to get the last glitches out. The 0.2mm layers are looking good, also the amount of filament and the temperature.
Mayor problem is the warping. Its a known problem when printing ABS. PLA would be easier but because we wanted to print a second printer we needed ABS.
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